Did the service this morning. Took me awhile as I got stuck on the dang torx screw that holds the filter as the exhaust was in the way lol. I tried as hard as I could to use the parts from autozone but they don't have it straight in their computer so I went with the advance auto pro king kits. (PK-330 & PK 331) <<that's both filters and the gasket. Also bought 8 qts of castrol ATF 4+ or whatever it is called....
I jacked up the front of my truck a little (my step bars hang low and my big belly doesn't fit lol)
This is the hardest part....no drain plug, so try and drain the pan without making a mess, I did it slowly and didn't spill a drop.
Cleaned up the pan (there was no gasket it was RTV sealant).
Unscrewed the cooler line filter(wow it was tight). Screw on the new one as tight as I could by hand.
Now where I got stuck....the dang torx screw that holds the pan filter on I couldn't get to with my tools (I have limited options for torx) because of the exhaust crossover pipe....so I used a torx bit for like a screwdriver/drill and gripped it with channel locks and got it off (like 30 min lol). Pulled old filter out, installed new filter, made sure it seated well in the rubber ring (I did not swap the rubber ring). Reinstalled and tightened the torx screw the same way and got it snug then a turn or so.
Reinstalled pan and used the rubber gasket just due to ease and I plan on eventually swap the pan for an aluminum deep one so it'll be easier to clean. I set the gasket on the pan on the ground and pushed the screws through to hold the gasket in place, then put it on.
Couldn't maneuver a torque wrench well in the area so tightened in a criss cross pattern till the pan bolts were a little past snug, then torqued one to about 105 in lbs, then felt it with my ratchet, and made the rest match that "feel".
Poured in 4 or 5 qts, checked and it was barely touching the dipstick....poured another and the level was good. Started truck, put in each gear, then checked again, and took another 2 or so qts. You need to buy 8 qts.
I think I actually ended up putting in about 7.5 qts, and I slightly overfilled it. I checked it later after a drive and the trans temp was about 160 deg F, and it was like an 1/8 inch or so about the high mark when hot (it says hot is 180), so it is a little overfilled. Will this hurt it? I can suck some out if need be, but if it won't hurt I'd rather leave it...
Oh I forgot, I also cleaned the magnet in the pan off then reinstalled it while the pan was out.
About $75 for all parts and fluids, that includes a can of cleaner and RTV(I will return for about $7).
Thank you all for all the help. Shifts maybe SLIGHTLY firmer, the old fluid was very red and smelled fine.
Anyone have any info on my slight overfill?